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Lake Mead Intake No. 3 Tunnel
(2010)Bericht IGTThe present report re-evaluates the stability conditions in the first 600 ft of the intake tunnel and presents possible solutions, which are statically equivalent but different from the construction schedule and cost point of view. The report serves thus as a decision making aid. Our favorite solution foresees a combination of low slurry pressure with advance drainage via long (as long as possible) boreholes, which are arranged outside ...Report -
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Lake Mead Intake No. 3 Tunnel
(2010)Bericht IGTFace instability represents one of the main potential hazards of the Lake Mead tunnel. The TBM is designed for being operated closed mode with a high pressure in the working chamber. The compensation of the hydrostatic pressure by compressed air or a pressurized slurry improves face stability considerably, but presents operational disadvantages particularly in the case of hyperbaric interventions in the chamber during standstills. For ...Report -